MadSci Network: Physics |
I think to answer this question I first have to explain what caused the TMI accident in the first place. The accident began about 4:00 a.m. on March 28, 1979, when the plant experienced a failure in the secondary, non-nuclear section of the plant. The main feedwater pumps stopped running, caused by either a mechanical or electrical failure, which prevented the steam generators from removing heat. First the turbine, then the reactor automatically shut down as they were supposed to. From the Nuclear Regulatory Commission web site: --------------------------------------------------------------------------- Immediately, the pressure in the primary system (the nuclear portion of the plant) began to increase. In order to prevent that pressure from becoming excessive, the pressurizer relief valve (a valve located at the top of the pressurizer) opened. (Again this was as the system was supposed to respond.) The valve should have closed when the pressure decreased by a certain amount, but it did not. Signals available to the operator failed to show that the valve was still open. As a result, the stuck-open valve caused the pressure to continue to decrease in the system. Meanwhile, another problem appeared elsewhere in the plant. The emergency feedwater system (backup to main feedwater) was tested 42 hours prior to the accident. As part of the test, a valve is closed and then reopened at the end of the test. But this time, through either an administrative or human error, the valve was not reopened - - preventing the emergency feedwater system from functioning. The valve was discovered closed about eight minutes into the accident. Once it was reopened, the emergency feedwater system began to work correctly, allowing cooling water to flow into the steam generators. As the system pressure in the primary system continued to decrease, voids (areas where no water is present) began to form in portions of the system other than the pressurizer. Because of these voids, the water in the system was redistributed and the pressurizer became full of water. The level indicator, which tells the operator the amount of coolant capable of heat removal, incorrectly indicated the system was full of water. Thus, the operator stopped adding water. He was unaware that, because of the stuck valve, the indicator can, and in this instance did, provide false readings. --------------------------------------------------------------------------- For a more detailed version of the TMI event and great information on nuclear power, I recommend: http://www.cannon.net/~gonyeau/nuclear/ What were the causes that allowed the accident to proceed this far? Primarily, poor operator training and instrumentation design. Improvements in these areas would have allowed the operator to recognize and properly correct the problems in the plant before they proceeded to the point of damage to the nuclear reactor core. It's my opinion that these are the fundamental causes of the accident along with the maintenance error that left the valve in the emergency feedwater system shut. Could the accident have been avoided? This is harder to answer. As outlined at the above web address, several changes to nuclear operations have been made since the accident: All electric utilities expanded significantly the training conducted for personnel who work at and support nuclear plant operations. This included establishing the National Nuclear Academy which accredits the plant training programs in 10 areas. Also, all utilities purchased simulators for training personnel who work in the main control room. Equipment changes included monitoring instrumentation capable of withstanding severe accidents and hydrogen recombiners. Personnel-related changes involved upgrading of training and qualification requirements and a requirement to have a degreed shift technical advisor assigned to each shift to evaluate abnormal conditions. The purpose of these changes was to avoid similar problems in the future. If these changes had been made earlier the TMI accident could have likely been avoided. If operators had correctly interpreted the indicators, had improved indicators, or had the maintenance error been avoided through better procedures and supervision, then the accident would have been avaoided. But, I am not sure if the need for these changes would have been recognized if the accident had not happened. Since nobody was hurt by the accident many people in the industry regard it as an expensive (since the power plant was a financial loss) lesson that has lead to great improvements in nuclear power plant operations. See the web address above or its links to get more information on those improvements. Michael Baker, Ph.D., P.E. Nuclear Engineer
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